|
Case Study #6
Application:
HVAC Heat Exchanger Assembly Lift
Assist
Problem: Customer was using an out of
date manipulator that caused them to manhandle the
part. The manipulator was bulky and slow resulting
in a task time that was unacceptable. Also, the
previous manipulator was only built to handle parts
that were quality acceptable. Hence, the operators
had to bend over with the manipulator to place the
rejected parts onto the ground. Lastly, the custom
tooling on the previous manipulator had nothing to
insure the parts would stay in place. If the part
was picked up and the tooling was moved too quickly,
the part could come loose with the potential to
cause injury.
Solution: We integrated a Gorbel zero
gravity, high speed PLC controlled servo driven
hoist (Gorbel G-Force) with a custom fork and vacuum
tool. The vacuum portion of the lifting tool was set
up to only release if the weight was removed from
the tooling. A custom proximity sensor ensures that
the product will not be released in mid-air. The
forks on the tool were rounded and coated with a
UHMW pad to avoid accidental product scratching. The
handle was built to float with the lift tool. This
kept the operators hands in good ergonomic positions
at all times, and solved the operators problem of
bending over to grab or set down the part.

This heat exchanger lift assist was integrated
with a Gorbel G-Force
for high speed precise placement.
Ergonomic Partners can come to your facility and
provide an on-site lifting demonstration of the
Gorbel G-Force. Please
contact
us today.
Case Study
Archive |